代码 oL1: Motor Overload
问题描述与安全警告
Yaskawa A1000 AC Drive 触发了严重的 Motor Overload 警报。需要由合格的操作员或维修技师立即处理,以防止在制造周期中对设备造成二次损坏或导致零件报废。在接触电气控制箱之前,请务必确保遵循标准安全和停机挂牌 (LOTO) 程序。
官方故障排除步骤
Code type: Fault Manual section: Yaskawa A1000 Troubleshooting Load is too heavy. Reduce the load. Note: After the value of U4-16 has decreased to one less than 100, reset oL1. The value of U4-16 must be less than 100 before oL1 can be reset. Cycle times are too short during acceleration and deceleration. Increase the acceleration and deceleration times (C1-01 through C1-08). A general purpose motor is driven below the rated speed with too high load. - Reduce the load. - Increase the speed. - If the motor is supposed to operate at low speeds, either increase the motor capacity or use a motor specifically designed to operate in the desired speed range. V/f characteristics (voltage and frequency) are not suitable Set the V/f pattern setting parameters (E1-04 to E1-10) to match the motor characteristics. The wrong motor rated current is set to E2-01. - Check the motor-rated current. - Enter the value written on the motor nameplate to parameter E2-01. Multiple motors are running off the same drive. Disable the motor protection function (L1-01 = 0) and install a thermal relay to each motor. The electrical thermal protection characteristics and motor overload characteristics do not match. - Check the motor characteristics. - Correct the type of motor protection that has been selected (L1-01). - Install an external thermal relay. The electrical thermal relay is operating at the wrong level. - Check the current rating listed on the motor nameplate. - Check the value set for the motor rated current (E2-01). Motor overheated by overexcitation operation. - Overexcitation increases the motor losses and the motor temperature. If applied too long, motor damage can occur. Prevent excessive overexcitation operation or apply proper cooling to the motor. - Reduce the excitation deceleration gain (n3-13). - Set L3-04 (Stall Prevention during Deceleration) to a value other than 4. - Set n3-23 (Overexcitation Operation Selection) to 0 (disabled). Speed Search related parameters are set incorrectly. - Check values set to Speed Search related parameters. - Adjust the Speed Search current and Speed Search deceleration times (b3-02 and b3-03 respectively). - After Auto-Tuning, enable Speed Estimation Speed Search (b3-24 = 1). Output current fluctuation due to power supply loss Check the power supply for phase loss.
Source: Yaskawa AC Drive A1000 High Performance Vector Control Drive Technical Manual (SIEP C710616 21H)
Last reviewed: 2026-07-01 · Verified against the manufacturer’s official documentation.
关于 Yaskawa A1000 AC Drive 警报
由 Yaskawa 制造的工业控制器具有广泛的诊断系统,用于保护内部电路和机械连杆。当 A1000 AC Drive 出现类似 oL1 的错误代码时,通常表示指令值与实际传感器反馈之间存在不匹配。
完整报警清单: 280 Yaskawa A1000 AC Drive 代码s.
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